eBay, will I ever learn?

I bid on a SPI combination square, and got it for $50.

Now that is a pretty good deal. Looking in the machine tool catalogs, I found it for $148,$151, & $158. So, I can’t have any complaints for $50, heh?

OK, this is the Hardened Steel 4 piece set with the square head, the center head, and the protractor. It  also has the Engineering scale on the ruler, which has the 100th inch scale rather than the 64th inch of the carpenter’s version. Just what I was looking for.

But, with my eBay luck, it arrived missing the centering head (on the left in the above photo). I contacted the seller, and he said he was sorry, and promised to send me the head. Today I received the center head, so no problems, heh?

Well, you forgot my eBay luck, he sent me the cheaper cast iron head instead of the hardened steel head that comes with the set. The cast iron set is about $30 cheaper than the hardened steel head and if you drop the iron heads on the shop floor they tend to break. Maybe, if I send it back he will send me the correct one, but I am real tired of hassling with eBay sellers, so I guess I will just keep it as is, and put this seller in my list of folks not to buy from again.

On a more positive side, I got some stuff I ordered from amazon.com, including a dial indicator set that has the magnetic base a 0-0.001 dial indicator with a 22pc head set (I do not know what I need that for), and a 0,015-0-0.015 dial test indicator (I do know what to use it for).

You use it to show variations in a measurement. In this photo you can see it measuring the runout on that shaft. The shaft there has a runout of -0.0 to +.0005 of an inch. about an inch from the chuck. Pretty good, but not phenomenal. However, it is small enough that you can not see any wobble at the end of that 5″ shaft when you turn the chuck.

PayPal decided against me on the lathe deal, I had asked for a $135 refund. off the $370 I paid the guy for a supposedly working lathe. The $135 was what I had to pay for the parts needed to put the lathe back into working condition. I did not ask anything for the approximately $250 worth of work involved. I would have been far better off buying a brand new lathe from Harbor Fright for $499 + $6.99 shipping. At least this was a “live and learn” situation, rather than the guy outright deliberately cheated me.

Now, with amazon.com, if something is wrong with what you buy, they will provide a prepaid return shipping label, and as soon as they have the tracking number, refund your money or ship out a replacement. They are a joy to buy from.

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Happy New Year

May 2012 be the best year so far for all my readers.

About the only thing that has happened between the holidays, is I received the cutters that fit for the lathe. To check them out I faced off about 1/3 of a 1/4×20 nut. I have been showing people it as a $500 nut ($0.04 for the nut, plus $500 for the tools to do it). Of course the value will drop a lot as soon as I turn something else (grin).

The new credit card is handy for keeping some money in the bank. I do not have to pay it out until I get the next check from Social Security. Speaking of which, they finally gave me a raise, all of $27 a month, after none for the past three years while the cost of living continued to increase insanely.

It does not look like I am going to hit my 250 word minimum for this post.

 

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Merry Christmas, Yuletide, Return of the Sun, whatever…

The holiday is upon us this Christmas Eve Day.  I want to wish all my readers the best of season’s greetings, and to all kids, from 1 to 101.

Looks like there is not much possibility of a White Christmas here. In the 40′s today, and supposed to be 50F tomorrow. In fact, we have only had one snow to amount to anything this winter so far, about one inch overnight, and that melted the next day.

I got a full refund on the view camera, but of course I do not now have a view camera.

I am in a PayPal dispute about the lathe. I asked for a refund to cover the parts I needed to repair the lathe, less a new chuck. I feel that is more than fair. But, one does not know how PayPal will decide on this. If they decide against me, it will be the first time that has happened. I do try to be very honest about these things.

I am having a problem getting cutters that work properly on the lathe. The ones in the kit were too long, a set of 3/8″ indexable cutters were too fat (I bought them from Amazon so it was not problem returning them), I now have  a set of 1/4″ indexables on order.

Intexable tools are ones that have a tool holder and replaceable carbide cutters  that can be replaced without removing the tool holders, so they do not change position. The particular ones I ordered use a 60-60-60 degree triangular cutter that give you 6 cutting edges before you have to replace the blade. The 5 holders hold them at 30-60-90-120-150 degrees, and all use the same cutters.  Those give you two forward facing cutters, a straight on cutter, and two rear facing cutters.

Of course sometimes you need something different, and for those times I will use high speed steel cutter that I can grind to the shape I need. Some folks swear that those are the only way to go for a hobby lathe, but it seems to me, that for general use, I do not want to spend a half-hour grinding a cutter sharp every time I want to ust it.

Let’s see, I bought a 1/2″ keyless chuck that turned out to be too long, but I was able to swap it with the regular chuck on the drill press.

I also got a milling slide for a Taig lathe. It will allow me to do some minor milling on the lathe, but only has a couple of inches of travel. So, once I figure out how to mount it I will be able to mill stuff as long as it is not bigger than 2 x 2.5 inches.

I bought a headboard for my bed, finally. I have been watching for a solid wood one finished on both sides for a long time; since I moved into this apartment, actually. This one showed up at Good Will for only $15. It is solid wood, 4×4 uprights, with a 27 inch tall, one inch thick, center. It weighs about 50 pounds. Turned out to be for a queen sized bed, but my bed is a regular double sized one. I bolted a board across the legs and bolted the bed frame to the board.  Now when I sit up in bed to read, the bed does not roll away from the wall.

I guess all that stuff can be considered my Xmas presents; in which case, I have receive a lot more this year than I have in the past several years.

In my Shamanic capacity, I have carefully determined that the Sun is on its way back. So, let the feasting begin.

 

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A New Saddle and Hand Wheel for Lathe

My, hopefully, last order of parts came, and I replaced the saddle and hand wheel. As you know from a previous post the old saddle was abnormally worn. The old hand wheel was cracked at the set screw hole and had a big chip out of it, more a cosmetic problems on it than anything else.

Installing the new saddle I realized something that I had not seen anywhere about how the retainers were adjusted.

PHOTO

In the photo above (that is the old saddle used for illustrative purposes) you see that there are three hex-socket cap screws and two set screws with lock nuts on them. Most of what I have read on the web says you adjust the set crew for the proper clearance by fiddling with them a lot and then tighten the cap screws. Only, that is not the way to do it at all.

Instead, ignoring the hex sockets in them, tighten down the cap screws with your fingers until they are just starting to snug up. Check that the retainer strip is level with even spacing (we are assuming that no one had destroyed you lathe yet by improper adjustment, if they have you nay not be able to level the retainers).

Move the saddle back and forth on the ways. Does it slide easily without being able to wobble it? It should not be able to rotate noticeably in any direction, but should move back and forth freely. If it does not do that, tighten or loosen the cap screws a smidgeon with your fingers. We are talking something like a sixteenth of a turn here.

Check it again, and readjust again if needed. When you have it just right, using a hex key turn in the set screws until they are just slightly tight. That will put tension on the cap screws so they will not loosen. Then holding the set screws with the hex key so they can not turn, tighten down the lock nuts.

Check that everything is still OK, if not back everything off and do it over.

To double check everything, put a few drops of oil on the ways and run the saddle back and forth. If everything is OK, the oil should spread out evenly. Remember, that the saddle actually rides on the sloping sides of the rail, and about the rear half-inch of the bed.

Congratulations, you have just set your saddle retainers exactly right without bending them, cracking them, or warping the saddle.

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I Lied!

 

I said sometimes you do OK on eBay. I lied. Now that it is  dark I used a flash light to check the bellows on the camera. It looks like a christmas tree.  Unfortunately, this is not one that has interchangable bellows.

I am about to write the seller to see what he is going to do about that.

 

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Monorail view Camera, or sometimes you do OK on eBay

ADDED 12/9/11: Turned out the bellows are bad, see next post “I Lied”.

 

Well, this one should go on Graywolf Photo, but the subtitle makes it appropriate here, I guess

Today I received an Omega E View Camera from a guy on eBay.

It came as a second chance offer, because the wining bidder backed out of the deal. Now one thing about that is, I really should have got it for my minimum bid, because there were only the two of us who bid on it, but since my maximum bid was only $7 higher, I did not argue about it. At first I thought one of the riser knobs and gear was missing, but I found it in the bottom of the box; I guess it fell off in shipping.

The lens is mine, the seller included two lens boards with the camera and some out dated 4×5 film. The previous photo was done with flash, this and the rest with the overhead light.

That is how the camera was set in the previous photo. This one came out nice and sharp.

For some strange reason the Olympus C-5050z does not want to focus on the lens. Did I ever say, “I hate autofocus”? That is the old lens from my Crown Graphic, the one with the damaged syncronizer, but if I remember correctly, it still works on X sync. Just goes to show you should never toss anything out. That 135mm lens looks like it is about the shortest that will work comfortably on this camera. Since that is about the same as a 35mm lens on a 35mm camera, I can live with that. If I can find something around 200mm when I have some spare money, I would be very happy.

In the above photo you can see the partial boxes of film on top of the TV that the seller tossed in with the camera. Not bad for $107 + SSH.

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It’s Working

The parts for the lathe arrived today, for the past couple of hours I have been working on it, with the result that everything seems to work. I ran it to and fro with the power feed (if I ever figure out how to post a video I will put one up of it working), and the slide moves back and forth easily. I also managed to get the saddle working in what seems to be a satisfactory manor for the time being.

Above is the problem with the saddle. If you look at the right end of the groove you will notice that it is worn to a curve. That allowed the saddle to rotate a bit, which would have made it very difficult to machine anything to tolerance.

That was caused by over tightening the ends of the retainers. In the photo above you can see how worn the ends of these retainers (way gibs) are. What I did to try and fix that problem was run a file along the side of the groove to make a longer straight section to keep the saddle from rotating. About 3/4 of the groove is now straight, but there is no further room for adjustment as the retainer is flat against the saddle.

The other main problem was the broken off leadscrew support. If you compare the above photo with the following one that has had a new support installed you will unerstand what I am writing about.

With that fixed, the power feed will now work with out skipping.

I also now have the change gears that allow me to cut screw threads on the lathe using that power feed,  and the hand tools that came with the lath when new.

As soon as the cutters get here, I will do some experimental machining to make sure things are accurate and correct.

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Further Adventures of A Fool (more lathe woes)

While waiting on my parts, I pulled the saddle and did some checking. Not a happy camper here, because someone had, as I mentioned, ran the lathe without the middle screws in the way gibs; which, pulled down the ends of the saddle and wore them badly.

Worn Lathe Saddle

Notice the gap on the left side of the guide rail. That gap allows the saddle to rotate a bit back and forth (rocking in the horizontal plane). Something like that will never allow accurate machining.

I have no choice but to order a new saddle for the lathe. That puts the price I have paid over the price of a new lathe. I guess I have to consider this a learning experience. What have I learned? Never buy a used machine tool unless the price is less than ten-cents on the dollar. I could have bought a new 7×12, next model up, for $570 shipped: when I order that part, and the others I put off as not immediately needed, I will have $572 in this one.

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& Yet More About the Lathe

I got a reply from the seller. To paraphrase: “I didn’t know it was junk, so it isn’t my fault”.

Or, in his own words:

“As I said in the ad; The only thing I checked is if the machine turned on. Which it did. It was clean, lubed and appeared to be lightly used. I’m sorry to hear of all the other problems you have apparently encountered with the unit, as I did not know they existed. I’m happy you can acquire the needed parts. Evidently, your a machinist, I’m not. I just bought the machine to do one project, and it was to small. I never even bought any tooling. The guy I bought it from got it from an auction. So, what I got is what you got.”

The following is what I have just ordered to fix the lathe to the point where it will run. The free stuff is parts that come with the lathe that the guy I am buying the parts from tossed in for free. To put the lathe in “out of the box” condition, I would have to order another $80 worth of parts from Mike. Mike sells on eBay  (macnc11). Ever inquired about something from an eBay seller, and have him telephone to see exactly what you were looking for? Mike did. 1000% (yes I typed three zero) recommended. I guess this proves that some days you lose, and others you win.

Description Quantity Unit price Amount
Leadscrew Support #270 - Mini Lathe ref. 1 $9.22 $9.22
Saddle Retainer #92 - Mini Lathe ref. 2 $6.07 $12.14
Half Nut#75 - Mini Lathe ref. 1 $0.00 $0.00
MT2 Short Live Center #143 - Mini Lathe ref. 1 $15.39 $15.39
Change Gear Set of 10 - 30, 35, 40, 40, 45, 50, 55, 57, 60, 65 Tooth Size 1 $34.00 $34.00
Hex wrenches, set of 4 (#311) - Mini Lathe ref. 1 $0.00 $0.00
Spanner, 8-10 (#312 - Mini Lathe ref. 1 $0.00 $0.00
Oil Can (#310 - Mini Lathe ref. 1 $0.00 $0.00
Spanner, 14-17(#313 - Mini Lathe ref. 1 $0.00 $0.00
Description (optional) 1 $0.00 $0.00
Subtotal $70.75
Shipping/handling $11.65
Total $82.40 USD

Note to recipient

I’m including #75 Half nut “No Charge”, it can be made to work if you choose, the pin needs to be moved toward the center, also the #313(14-17)wrench. I can have these in the mail today. Thanks —–Mike

 

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And Sometimes We Are Lucky

Started tearing the lathe down to see what was what inside the headstock. Stripped the lathe down piece by piece until I took off the motor cover. What’s this? They motor is not supposed to be mounted at an angle!

Turns out all the motor mount nuts were loose. The funny sound I was hearing was the toothed pully moving against the toothed belt. I tightened up the motor mounts nuts set the proper slack in the belt, plugged it in and turned it on.  The proper parts spun, remember all the gear train had been removed. Installed the bits to drive the spindle, and… it turned smoothly like it should.

So, I put the gear train back on and a couple of the covers….

Partially reassemble lathe

With the gear train back on, where I stopped for the evening (see above photo), I tried running it again. Everything so far is working smoothly. Tried it in forward and reverse, and then again with the lead screw (a long screw that provides power feed to the carriage)  engaged.

Great, so I am not going to have to spend $60 on transmission gears right away.

For some of the other parts I am waiting on a quote from a guy that buys returned ones from Harbor Freight,t and strips them for parts. Only problem is, he does not want to sell bits and pieces, but whole sub-assemblies. So, for instance I can get a thread cutting change gear set from him, but not an extra 50 tooth gear that I want for cutting metric threads.

This is better than I thought it was going to be this morning, but still not a happy making thing. But, I now guess that it will only be about 1/2 what I thought it would to fix the lathe. In other words I will have in it about what a really nice, not a bargain, used one would  cost.

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